Well some good progress yesterday and today

the car is back on all 4 wheels finally....
So the hunting wasn't an air lock I will try and explain the root cause. So as soon as the car got warm it started to hunt from 500rpm to 2.5k rpm just a steady bounce. We bled and bled the system to no avail so we looked elsewhere as we had last week. So there was no vac leak which we could easily test by covering the inlet throttle body and the engine cut out, basic but it tells us a definitive answer. So we were really starting to struggle when we disconnected the IACV sensor the hunting then stopped we got a cel but no hunting as a side effect the car sounded rough not bad but not as a clean tick over as you would expect. We then reconnected the sensor and the hunting returned? We powered off the car disconnected the battery to reset the ecu. Once reconnected we restarted the car this time we removed the temp sensor that connects to the end of the inlet chamber on the righthand side if you are looking straight on from the front of the car. This had the same result a cel a rough idle but no hunting?? We did the disconnect and reconnect of the battery and tried the same again with both sensors on and off in different orders and together with the same results, once put back to normal the hunting retuned.... So we somehow deduced it had to be the IACV as this is the only electronically controlled part of the throttle body workings. We removed it and other than being a tad mucky it all looked ok. Whilst rummaging through the spares box we found another h22 IACV so we fitted that as it looked in good order and low and behold car ran without an issue!??!?!
So not entirely sure what was wrong with the original IACV but something was a miss?
To note we have done a vacuum loop/delete and the coolant bypass.
Either way the car run perfect other than the timing and idling which needs tuning correctly by a pro not us

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So after that we run the car got it to temp and decided to drop it and test the gearbox as shown below:
https://youtu.be/RNgnFy7YL8c
After the test we have found another coolant leak but this should hopefully be a much easier fix.
We also fitted 15mm hub centric hubs to the front which required the original studs to be shortened to 2cm each but made the fronts fit perfect. hopefully tomorrow I can check the rears to see whether to order 15 or 20mm hub centric spacers?... I will use the old basic spaces to judge which to get.
So still a lot to do but the gearbox and clutch work so thank you to the seller's I got them from for there honesty, tbh the clutch felt and bit like new
To do
Shorten the air intake pipe as the filter is hanging lower than the engine
Fix water leak
Secure all loose hanging harness bits
Rewire the hids
Refit the bonnet hopefully it shuts lol
Take it for some test runs
Get the timing tuned by a pro
There is a lot more to do also but i am not listing everything